I stole this pic from a website....too hard to get one but if you zoom in on the one above you will see the flock.
Travel days 5-9 took us to Spring Brook Marina in Seneca, Heritage Harbor in Ottawa (very nice facility...stayed a couple days), Illinois Valley Yacht Club in East Peoria (very welcoming club members and a nice facility), the Lodgston Tug Service barge in Beardstown (yes, just a working barge full of cables and pipes along the river's edge with no electricity or other facilities....but as they say, any port in a storm), and finally to the Alton Marina where we did catch up to our friends on JimKat.
Sunrise departure
My turn to lead.
Foggy pass.
Ivy Club
A pass on the one whistle.
We really cranked it up on day 9 and covered 104 miles! We had a nice push from the river current and travelled close to 17 knots a good portion of the trip to Alton which is a great stop. Everything floats. Pool, buildings, etc. Note the height of the pilings for the docks!
We rented a car and went to the Arch in St Louis one day. Took the ride to the top of the arch. What a view! Had a great lunch on the garden level at the Four Seasons before returning to the marina. Then a grocery run to Schnucks (very nice store) and some laundry duties.
The ride up
View from the top
Nice restaurant view too
Another day our friends Jim and Kathy (JimKat) offered to drive us to Grafton for a short visit. We had passed that marina on our way to Alton and remarked that it looked like a cute town. And we remarked that "you can't stop everywhere" so we were excited to get to see it. But.....the morning engine room check getting ready for tomorrow's departure found a quart of oil in the drip pan on the port side and coolant down as well. So we called CAT for service and Tim showed up a few hours later to diagnose. The oil leak was the Walker Air-Sep crankcase ventilation system. The fitting on the bottom had been bent over (my assessment is this happened during all the work done by CAT over the winter) and was leaking some of the oil it was supposed to return to the oil pan. So Tim straightened, added sealant and reinstalled. The coolant pressure test suggested the system is OK. But the couple quarts of coolant went somewhere so I will just have to continue to watch it. Hopefully the oil samples taken will confirm no issue in a few days. So we should be good to go tomorrow.....a few BOAT dollars later that is. We only have 45 miles (and two locks) to go tomorrow.
The next few days will be challenging with three nights of anchoring due to no facilities along this portion of the trip. Hopefully we do not get windy nights. So no posts... and likely no AIS tracking of where we are for all you stalkers either!! :-)
4 comments:
Very interesting. Keep the updates coning. Enjoy the nice weather.
Keith
Thanks for following!
Hi Tom,
I don't think my prior comments made it so I'll try again. Sorry to hear about Julie's Mom! After a rough start, looks like you've been making good progress! I hope the eye and the shoulder are doing well. Thanks for the updates! Take care!
Love the updates. Good thing you're not on Lake Huron anchored as she's roaring pretty good. Hopefully you didn't get winds while you were anchored.
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